Today the team worked on modifying the VEX Robot to improve its efficiency. Tank treads were applied over the original wheel and a small gear was replaced due to it being mauled during one of our tests. We have also begun searching for code that will allow the VEX Robot to be fully automated. Discussions have also been held about a future competition we could have with the AM class.
Quick design of a possible attachment modification : 3D design Smooth Lappi-Jaiks | Tinkercad
(Will continue to make more attachments and see which is best)
Next steps...
- Continue our search for code that allows our VEX Robot to become fully automated'
- Create a device that will prevent the VEX Robot from falling backwards when braking
- Continue designs on TinkerCAD
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